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| [#1] 5687牛輸出前級(Baker.Steven) 牛輸出前級,重中之重當然是輸出牛,比利時Monolithic Magnetic ,Nanocrystalline core 當然是首選,接4:1,次級並1K電阻,初级反射抗阻16K,牛前線路简潔.只需要pot 條loadline,揀個理想工作點,計返粒陰極電阻數值就OK,呢次部機做dual mono,牛都2隻,Vol & Selector架都分開2隻,電源穩壓就用Diytime出品,裝製無什麼難度,唯一喺金工對位要準確D! ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:17 | |
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| [#2] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:18 |
| [#3] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:19 |
| [#4] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:19 |
| [#5] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:20 |
| [#6] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:21 |
| [#7] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:21 |
| [#8] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:22 |
| [#9] 5687牛輸出前級(Baker.Steven) . ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:22 |
| [#10] 5687牛輸出前級(Baker.Steven) 網友部EML-300Bxls後級,亦都同時升级,換上同廠Amorph芯輸出牛! ![]() |
Baker.Steven 203.xxx.xxx.196 |
2024-10-29 11:30 |
| [#11] 5687牛輸出前級(Baker.Steven) 正....! 高手~ |
jcyc348 202.xxx.xxx.114 |
2024-10-31 13:16 |
| [#12] 5687牛輸出前級(Baker.Steven) 刚刚睇到呢個post,想問吓制作概念 1. 請問綠色訊號線係乜型號?旁邊对喇叭乜型號? 2. 用5687 接4:1前級牛只得3至4倍gain, 點解唔用你之前隻EC8010 可以出正常gain 3. 300B 或300B 变種胆,用兩級common cathode 6SN7其實已經夠哂gain做合併機,可以用passive volume 令訊號純度更高,請問加多部前級声音是否有其他变化而透明度及純度也有变化 最後修改時間: 2024-10-31 15:53:36 |
niceday009 59.xxx.xxx.45 |
2024-10-31 15:37 |
| [#13] 5687牛輸出前級(Baker.Steven) >>次級並1K電阻 隻Monolith 牛次級如果唔並1k电阻係得唔得,抑或佢指定要电阻termination(有D牛overshoot ),唔並loadline係打横失真更低 如果唔一定要並电阻,5687係在A1工作佢只係需要望到足夠初次电感,幾K:幾K其實係冇意義,唔並次級电阻等於隻5687在constant current 工作而load 係極高阻抗綫性更高 最後修改時間: 2024-10-31 16:18:35 |
niceday009 59.xxx.xxx.45 |
2024-10-31 16:01 |
| [#14] 5687牛輸出前級(Baker.Steven) Hi Mr. Steven Baker, I tried to guess what the schematic could be for your new 5687 line amp. I worked out the following schematic. Most likely it is different from yours. Johnny ![]() |
johnnykmtang 70.xxx.xxx.22 |
2024-10-31 21:26 |
| [#15] 5687牛輸出前級(Baker.Steven) 1K termination in transformer secondary may cause the loadline to be significantly tilt, 5687 not beneficial to have constant current load If there is no overshoot ringing in 10kHz square wave, I would say. to leave the secondary not terminated In case obvious overshoot is detected, put in place the snubber network , 330p in series of R, it reduces the burden of secondary load (1K is heavy)and make loadline horizontal, Lundahl always recommend sunbber network 最後修改時間: 2024-10-31 23:12:09 |
niceday009 182.xxx.xxx.113 |
2024-10-31 22:45 |
| [#16] 5687牛輸出前級(Baker.Steven) #14 Johnny 兄,請問您模擬後結果?1K用與唔用,性能分别如何?另外小弟只以用半支5687,工作設定與附圖一樣! |
Baker.Steven 203.xxx.xxx.196 |
2024-11-01 10:12 |
| [#17] 5687牛輸出前級(Baker.Steven) Hello Steven Baker, Good to hear from you. I experimented number of interstage, line output and input transformers. I realized that having a low impedance resistor as load would cause a bit higher in distortion and less dynamic. The sound image opens up a lot without the resistor. However usually there's a high frequency response at around 20~30KHz which can be damped with use of an RC network. What model of the Monolith Line output transformer you are using? The 20mA one? Johnny |
johnnykmtang 70.xxx.xxx.22 |
2024-11-01 10:27 |
| [#18] 5687牛輸出前級(Baker.Steven) I upgraded my parallel 6DJ8 - Monolith amorphous SLA-02 20mA line ouptut transformer configured 2:1, with 5842Q tube. B+ 120Vdc, idle current of 10mA. I notice 5842Q (417A) tube is more linear than 6DJ8 and with even higher gain. Real cool. Johnny 最後修改時間: 2024-11-01 10:41:10 |
johnnykmtang 70.xxx.xxx.22 |
2024-11-01 10:39 |
| [#19] 5687牛輸出前級(Baker.Steven) Johnny 兄,小弟用SLX-01/20,另外想知道您是否用cathode CCS? |
Baker.Steven 203.xxx.xxx.196 |
2024-11-01 12:05 |
| [#20] 5687牛輸出前級(Baker.Steven) Hi Steven, I use the simple transistor "shunt regulator" to provide the cathode voltage for bias of the tube. ![]() |
johnnykmtang 70.xxx.xxx.22 |
2024-11-01 16:36 |